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Oil & Gas Drilling

Industry Served: Gas, Oil & Petrochemical
Problem:

Chesapeake Operating, Inc., a major oil and gas drilling company headquartered in Oklahoma, uses a Hydra-Cell triplex diaphragm pump (3.5” stroke, 450 rpm max speed, 27 gpm max. flow rate, 4500 psig max. pressure) to pump saltwater (1.13 sg). The pump is located over 100 feet from supply tanks. The supply line comes out of the tank, goes underground across a driveway/parking lot for more than 100 feet, then up out of the ground into the inlet of the pump. While the pump operated adequately, the pump inlet gauge fluctuated +/- 7 psig and steel pipes next to the fiberglass supply tank vibrated so violently the customer was concerned the tank would rupture.

Solution:

A Blacoh model J4040V, 5 gallon suction stabilizer was installed on the inlet side of the pump. Suction pipe vibration stopped and fluctuation on the inlet pressure gauge decreased to +/- 1 psig. The customer is very pleased.

Result: